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Modifying an "O2-Cool" battery fan to (also) run from 12 volts

By: KA7OEI
19 July 2023 at 07:05

A blog posting about a fan?Β  Really?

Why not!

Figure 1:
The modified fan on my cluttered workbench, running
from 13 volts.
The external DC input plug is visible on the lower left.
Click on the image for a larger version.

This blog post is less about a fan, but is more of example of the use of a low-cost buck-type voltage converter to efficiently power a device intended for a lower voltage than might be available - in this case, a device (the fan) that expects 3 volts.Β  In many cases, "12" volts (which may be anything from 10 to 15 volts) will be available from an existing power source (battery, vehicle, power supply) and it would be nice to be able to run everything from that one power bus.

Background

Several years ago I picked up a 5" battery-operated DC fan branded "O2 Cool" that has come in handy occasionally when I needed a bit of airflow on a hot day.Β  While self-contained, using two "D" cells - it can't run from a common external power source such as 12 volts.

Getting 3 volts

Since this fan uses 3 volts, an obvious means of powering it from 12 volts would be to simply add a dropping resistor - but I wasn't really a fan of this idea (pun intended!) as it would be very wasteful in power and since doing this would effectively defeat the speed switch - which, itself is just a 2.2 ohm resistor placed in series with the battery when set to "low".

The problem is that the fan itself pulls 300-400 mA on high speed.Β  If I were to drop the voltage resistively from 12 volts (e.g. a 9 volt drop) - and if we assume a 300mA current - we would need to add (9/0.3 = ) 30 ohms of series resistance to attain the same speed on "high" as with the battery.Β  The "low speed" switch inserts a 2.2 ohm resistor, and while this works with its original 3 volt supply, adding this amount to 30 ohms would result in a barely noticeable difference in speed, effectively turning it into a single-speed fan.Β  By directly supplying the fan with something close to the original voltage, we preserve the efficacy of the high/low speed switch.

Fortunately, there's an answer:Β  An inexpensive buck converter board.Β  The board that I picked - based on the MP1584 chip - is plentiful on both EvilBay and Amazon, typically for less than US$2 each.Β  These operate at a switching frequency of about 1 MHz and aren't terribly prone to cause radio interference, having also been used to power 5 volt radios and even single-board computers (such as the Raspberry Pi) from 12 volts without issues.

These buck converters can handle as much as 24 volts on the input and provide up to 3 amps output - more than enough for our purpose - and can also be adjusted to output about any voltage that is at least 4 volts lower than the input voltage - including the nominal 3 volts that we need for the fan.

An additional advantage is the efficiency of this voltage conversion.Β  These devices are typically 80% efficient or better meaning that our 300 mA at 3 volts (about 0.9 watts of power) would translate to less than 100mA at 12 volts (a bit more than a watt).Β  Contrast this to the hypothetical resistive dropper discussed earlier where we would be burning up nearly 3 watts in the 30 ohm resistor by itself!

Implementation

One of my goals was to retain the ability of this fan to run at 3 volts as it would still be convenient to have this thing run stand-alone from internal power.Β  Perhaps overkill, but to do this I implemented a simple circuit using a small relay to switch to the buck converter when external power was present and internal power when it was not, rather than parallel the buck converter across the battery.

If I never intended to use the internal "D" cells ever again I would have dispensed with the relay entirely and not needed to make the slight modifications to the switch board mentioned below.Β  In this case I would have had plenty of room in the case and freedom to place the components wherever I wished.Β  In lieu of the ballast of the battery to hold the fan down and stable, I would have placed some weight in the case (some bolts, nuts, random hardware, rocks) to prevent it from tipping over.

The diagram of this circuitry is shown below:

Figure 2:
Diagram of the finished/modified fan.
On the left, J1 is the center-positive coaxial power connector with diode D1 and self-resetting
resetting thermal fuse F1 to protect against reverse polarity.Β  The relay selects the source of power.
Click on the image for a larger version.

The original parts of are the High/Low switch, the battery and the fan itself on the right side of the schematic with the added circuits being the jack (J1), the self-resetting fuse (F1), D1, R1, the buck converter and the relay (RLY).

How it works:

When no external power is applied, the relay (RLY) is de-energized and via the "NC" (Normally-Closed) contacts, the battery is connected to the High/Low switch and everything operates as it originally did.

External power is applied via "J1" which is a coaxial power jack, wiring the center pin as positive:Β  The connector that I used happens to have a 2.5mm diameter center pin and expects an outer shell diameter of 5.5mm.Β  There's nothing special about this jack except that I happen to have it on-hand.

When power is applied, the relay is energized and the high/low switch is disconnected from the battery but is now connected, via the "NO" (Normally Open) contacts, to the OUT+ terminal of the buck converter.Β Β 

Ideally, a small 12 volt relay would be used, but the smallest relay that I found in my junk box was a 5 volt unit, requiring that the coil voltage be dropped.Β  Measuring the relay coil's resistance as 160 ohms, I knew that it required about 30 mA (5/160 = 0.03) and if we were to use 12 volts, we'd need to drop (12 - 5 =) 7 volts.Β  The resistance needed to drop 7 volts is therefore (7/0.03 = ) 233 ohms - but since I was more likely to operate it from closer to 13 volts much of the time I chose the next higher standard value of resistance, 270 ohms to put in series for R1.

Figure 3:
Modification of the switch board.Β  The button is
the positive battery terminal and traces are cut to
isolate it to allow relay switching.
Click on the image for a larger version.
The diode D1 is a standard 1 amp diode - I used a 1N4003 as it was the first thing that I found in my parts bin, but about any diode rated for 1 amp or greater could be used, instead.Β  Placing it in reverse-bias across the input of the buck converter means that if the voltage was reversed accidentally, it would conduct, causing the self-resetting thermal fuse F1 to "blow" and protect the converter.Β  I chose a thermal fuse that has several times the expected operating current so I selected a device that would handle 500-800 mA before it would open.

Modification to the switch board

The High/Low switch board also houses the positive battery contact, but since it is required that we disconnect the battery when running from external power, a slight modification is required, so a few traces were cut and a jumper wire added to isolate the tab that connects to the positive end of the battery as seen in Figure 3.

Figure 4:
The top of the board battery board. The
connection to the Batt+ is made by soldering to
the tab.
Click on the image for a larger version.
Near the top of the photo in Figure 3 we see that the trace connecting end of the 2.2 ohm resistor has been separated from the battery "+" connector (the round portion) and also along the bottom edge where it connects to the switch.Β  Our added jumper wire then connects the resistor to the far end of the switch where the trace used to go and we see the yellow wire go off to the "common" contact of the relay.

In Figure 4 we can see the top of the board with the 2.2 ohm resistor - but we also see the wire (white and green) that connects to one of the tabs for the Battery + button on the bottom of the board:Β  The wire was connected on this side of the circuit board to keep it out of the way round battery tab and the "battery +" connection.

The mechanical parts

For a modification like this, there's no need to make a circuit board - or even use prototyping boards.Β  Because we are cramming extra components in an existing box, we have to be a bit clever as to where we put things in that we have only limited choices.

Figure 5:
Getting ready to install the connector after
a session of drilling and filing.
Click on the image for a larger version.
In the case of the coaxial power connector, there was only one real choice for its location:Β  On the side opposite the power switch, near the front, because if it were placed anywhere else it would interfere with the battery or with the fan itself as the case was opened.

Figure 5 shows the location of this connector.Β  Inside the box. this is located between two bosses and there is just enough room to mount it.Β  To do this, small holes were drilled into the case at the corners of the connector and a sharp pair of flush-cut diagonal nippers were used to open a hole.Β  From here it was a matter of filing and checking until the dimensions of the hole afforded a snug fit of the connector.

Figure 6:
A close-up of the buck converter board with the
attached wires and BATT- spring terminal.
The tiny voltage adjustment potentiometer is
visible near the upper-left corner of the board.
Click on the image for a larger version.
Wires were soldered to the connector before it was pressed into the hole and to hold it in place I used "Shoe Goo" - a rubber adhesive - as I have had good luck with this in terms of adhesion:Β  I could have used cyanoacrylate ("Super" glue) or epoxy, but I have found that the adhesive bonds of these tend to be a bit more brittle with rapid changes of temperature, mechanical shock or - most applicable here - flexing - something that the Shoe Goo is meant to do.

Because this jack is next to the battery minus (-) connector, a short wire was connected directly to it, and another wire was run to the location - in the adjacent portion of the case - where the buck converter board would be placed.

Figure 6 shows the buck converter board itself in front of the cavity in which it will be placed, next to the negative battery "spring" connector.Β  Diode D1 is soldered on the back side of this board and along the right edge, the yellow self-resetting fuse is visible.Β  Like everything else the relay was wired with flying leads as well, with resistor R1 being placed at the relay for convenience.

Figure 7:
The relay, wired up with the flying leads.
Click on the image for a larger version.

Figure 7 shows the wiring of the relay.Β  Again, this was chosen for its size - but any SPDT relay that will fit in the gap and not interfere mechanically with the battery should do the job.

The red wire - connected to the resistor - comes from the positive connector on the jack and the "IN+" of the buck converter board - the orange wire is the common connection of the High/Low switch, the white/violet comes from the "OUT+" of the buck converter and goes to the N.O. (Normally Open) contact on the relay, the white/green goes to the N.C. (Normally Closed) relay contact and the black is the negative lead attached to the coil.

Everything in its place

Figure 8 shows the internals of the fan with the added circuitry.Β  Shoe Goo was again employed to hold the buck converter board and the relay in place while the wires were carefully tucked into rails that look as though they were intended for this!

Now it was time to test it out:Β  I connected a bench power supply to the coaxial connector and set the voltage of my external test power supply at 10 volts - enough to reliably pull in the relay - and set the fan to low speed.Β  At this point I adjusted the (tiny!) potentiometer on the buck converter board for an output of 3.2 volts - about that which could be expected from a very fresh pair of "D" cells.

Figure 8:
Everything wired and in its final locations.Β  On the far left is
the switch board.Β  To the left of the hinge is the relay with the
buck converter on the right side of the hinge.Β  The jack and
negative battery terminal is on the far right of the case.
Click on the image for a larger version.
The result was a constant fan speed as I varied the bench supply from 9 to 18 volts indicating that the buck converter was doing its job.

The only thing left to do was to make a power cord to keep with the fan.Β  As is my wont, I tend to use Anderson Power Pole connectors for my 12 volt connections and I did so here.

As I also tend to do, I always attach two sets of Anderson connectors to the end of my DC power cords - the idea being that I would not "hog" DC power connections and leave somewhere to plug something else in.Β  While the power cord for the fan was just 22 gauge wire, I used heavier wire (#14 AWG) between the two Anderson connectors so that I could still run high-current devices.

* * *

Does it work?

Of course it does - it's a fan!

The relay switches over at about 8.5 volts making the useful voltage range via the external connector between 9 and 16 volts - perfect for use with an ostensibly "12 volt" system where the actual voltage can vary between 10 and 14 volts, depending on the battery chemistry and type.

Figure 9:
The fan, folded up with power cord.
The two connectors and short section of heavy
conductor can be just seen.
Click on the image for a larger version.

Without the weight of the two "D" batteries, the balance of the fan is slightly precarious and prone to tip forward slightly, but this could be fixed by leaving batteries in the unit - but this is not desirable for long-term storage as leakage is the likely result.

Alternatively, one may place some ballast in the battery compartment (large bolt wrapped in insulation, a rag, paper towel, etc.) or simply by placing something (perhaps a rock or two) on the top.Β  Alternatively, since the fan is typically placed on a desktop, it is often tilted slightly upwards and that offsets the center of gravity in our favor and this - plus the thrust from the airflow - prevents tipping.


This page stolen from ka7oei.blogspot.com


[End]


An ultrasonic superheterodyne receive converter (e.g. "Bat Listener")

By: KA7OEI
31 October 2022 at 03:45

In the mid 90s I decided to throw together what I called a "Bat Listener" - a simple receiver used to convert ultrasonic sound down to the audible range.

Figure 1:
The exterior of the ultrasonic receiver, complete with fancy
labeling!
Click on the image for a larger version.

Two types of circuits:

There are two common ways to convert a higher (ultrasonic) signal to the audible range, whether this is done using analog or DSP (Digital Signal Processing) techniques.

Frequency division

There are several ways to do this, the simplest being the "divider" type which digitally converts ultrasonic frequencies to audible by integer division of the input to a lower frequency.

The problem with this simple approach is that it does not preserve the amplitude (loudness) of the original sound since it must take the input signal, amplify/convert it to a series of logic-level pulses - which loses any amplitude reference - and do a brute-force digital division.Β  Additionally, if there are multiple signals present, for the most part only the strongest one will be converted down.

Clearly, one cannot "tune" this type of circuit:Β  A signal at 40 kHz will always be divided down by a fixed integer amount,Β  Let's say that the circuit digitally divides by 32:Β  That 40 kHz signal will be at 1.25 kHz.

Additionally, the direct "A-B" frequency differences between ultrasonic signals is lost, instead being "(A-B)/N" where "N" is the number of divisions.Β  In other words, the relative frequency differences between signals is not preserved.

Heterodyne conversion

The other way to do this is to convert the frequency.Β  In this technique, two signals - the ultrasonic to be converted - and another generated by the device (the "local" oscillator) are mixed together.Β  The result is an arithmetic shift in frequency.

The biggest advantages of this method are the fact that that not only are the differences in frequency preserved (e.g. two tones 1 kHz apart at ultrasonic will appear as two tones 1 kHz apart at audio) but the relative amplitudes (loudnesses) of the received signals are preserved as well.

Frequency conversion:

I chose to build a heterodyning receiver to convert the input frequency to a lower one.Β  This can preserve the amplitude and frequency relationshipsΒ  - plus it is fully tunable, allowing one to choose the frequency range to convert to audible sounds - and since it is a simple conversion, multiple signals present will also be preserved.

When it comes to frequency conversion, there are two ways:Β  The simplest - direct conversion - would involve mixing a variable oscillator with the incoming signal and filtering/amplifying the resulting audio.Β  This has the advantage of being the easiest, and it is the method described in this article:

Β Β Β Β  April, 2006 QST article, A Home-made Ultrasonic Power Line Arc Detector - link)

While I could have easily built something like this a decade before the above article was published, as I'm sometimes wont to do I decided to make it a bit more complicated, constructing a superheterodyne converter.

While a direct-conversion receive simply mixes an oscillator with the desired signal to cause a frequency conversion, a superheterodyne receiver operates like a conventional AM or FM radio:Β  The desired signal is first converted to an IF (Intermediate Frequency) - and this IF is then converted to audio.Β  The advantage of the superheterodyne scheme is that filtering may be applied at the IF to limit the receive bandwidth - and since the IF is fixed, its width remains constant over the tuning range, just like that in a conventional radio/receiver.

Circuit description

Figure 2:
Schematic diagram of the superheterodyne ultrasonic receiver.
See text for a circuit description.
Click on image for a larger version.

As noted above, this circuit is more complicated than it needs to be, so make of it what you will!

VCO:

The heart of the unit is U1, the VCO (Voltage Controlled Oscillator) which uses the venerable CD4046 PLL chip.Β  Often used for frequency synthesis, we are using (only) the oscillator portion, which provides a linearly-tuned and fairly stable frequency source, adjusted by the voltage applied via R101 (and scaling resistor R102).Β  The values were chosen to provide an approximate frequency range of 125 to 185 kHz (more on this later) to allow tuning of audio signals from (ostensibly) 0 to about 60 kHz.Β  The actual tuning range is closer to 115-190 kHz as a bit of extra margin for the frequency range.

The only critical component here is C101 which should be a frequency-stable capacitor.Β  I used a polystyrene capacitor, but an NP0 (a.k.a. C0G) or silver-mica could be used, instead.Β  When I reverse-engineered this device, I noted that the marked capacitance value was unreadable, but back-of-the-envelope calculates indicate that a value of "about 150pf" should be in the ballpark.

R103, connected to the "R1" pin of U1, sets the approximate center frequency range while R104, connected to the "R2" pin - sets the lowest frequency - which important, since we want to constrain the tuning to 125-185 kHz.Β  Additionally, the low end of the tuning range was further refined by R102 on the "ground" side of the tuning potentiometer, which sets the minimum voltage that may be applied to the "VCOIN" pin.

The VCO output, a square wave, is buffered by U2, a hex inverter, and several sections are used to provide both a VCO signal and its inverted version to drive the mixer.

While the 4000 series CMOS chips throughout this receiver will happily run from 3-15 volts, they are operated from a regulated 5 volt supply - mainly to improve frequency stability and to provide a nice, stable voltage for a few other low-level circuits and to provide isolation from the main battery supply which will vary a bit, particularly at higher receive volumes:Β  This variance, if it gets back into some earlier stages, could cause instability of the receiver in the form of "motorboating" or some other type of feedback.

BFO:

Another circuit is the BFO (Beat Frequency Oscillator) which is used to convert the IF signal back down to audio - both being processes that we'll discuss shortly.Β  This uses an inexpensive 500 kHz ceramic resonator to form an oscillator using one of the sections of U2C, the signal being buffered by U2B.Β  This signal is divided-by-two using U3A, one half of a 4013 dual flip-flop - and then divided by two again using U3B, yielding a stable 125 kHz signal.Β  As with the VCO, two phases of this signal (normal and inverse) are available, this time using the "Q" and "!Q" outputs of the 4013.

Input signal path:

J1, a disconnect-type 3.5mm stereo jack is wired so that an internally-mounted electret "capsule" microphone is connected by default.Β  This microphone element (M301) is of the "2 wire" type or electret microphone in which a bias voltage is applied to the same pin from which audio is drawn - this voltage being applied via R301 from the 5 volt regulated supply.Β  The specific make/model of this electret element is unknown as it was selected from a small collection to find the best performer at ultrasonic.

At some point in the future, I'll replace this with a more modern MEMs microphone as described in Another article:Β  Improving my ultrasonic sniffer for finding power line arcing by using MEMs microphones - link.

The signal from the microphone is applied to U4A which is wired as a unity-gain buffer.Β  For this, an LM833 is used, an inexpensive, low-noise dual op amp:Β  An LM358 or many other types may be used here as well - just make sure that it is is fairly low noise:Β  I'd avoid the use of the LM1458 here as it is quite noisy by comparison!

Section U4B amplifies the signal voltage by 10 (20 dB of power gain) and this signal is applied via R305 to a simple L/C high-pass filter consisting of C303, C304, L301 and L302 the latter two components being inexpensive 18 milliHenry inductors.Β  Certainly, an R/C-based high-pass filter could have been constructed using U4B, but I chose not to do that for some reason.

Figure 3:
Inside the ultrasonic receiver, constructed on
prototype board and having been modified
several times over the years.
Click on the image for a larger version.

In simulation, the C303/C304/L301/L302 filter has a -3dB roll-off of aboutΒ  23 kHz, it's down by 10dB at about 19.5 kHz, by 20dB at about 16 kHz and by 40 dB at 9 kHz and with the values shown, it's flat to within 1 dB between about 24 and 100 kHz.

The output of the filter is amplified by U5B - and then even more by U5A (which has a bit of roll-off from C307) to yield a whole lot of gain.Β  It's very possible that I over-did the gain here, but unless the signal source is quite close, there is no clipping observed on the output of U5A.

Its worth noting that a mid-supply voltage is created using R309/R310 to provide a "virtual ground" for the op amps and to maintain stability, it is heavily filtered by C306 and C302, each located near the respective op amp shown on the diagram.

Mixer and band-pass filter:

It is this next section that may seem unfamiliar to some - the use of a CMOS analog switch as a signal mixer.Β  For this, a CD4066 is used which consists of four separate analog switches.Β  The filtered and amplified ultrasonic input signal from U5A via C308 is applied to pins 2 and 10 of U6A/U6D.Β  When the respective signals on the control pins "VCO_A" and "VCO_B" go high, the switches are activated, and because VCO_A and VCO_B are inverts of each other, each of these switches is closed in turn.Β  The result of this is that the inputted signal is chopped up at the rate of the 125-185 kHz VCO and this produces two mixing products.Β Β 

For example, let's assume that there is a 40 kHz signal is present on the input that we wish to hear.Β  If the VCO is tuned 40 kHz above the 125 kHz IF (again, more on that momentarily) - to a frequency of 165 kHz - the switching action of U6A and U6D produces both the sum (165 + 40 = 205 kHz) and the difference (165 - 40 = 125 kHz).

T301 is a filter/transformer that passes only the 125 kHz signal - the difference signal in this case.Β  This transformer consists of two separate windings, each resonated using its internal capacitors and the externally-added 820 pF capacitors on each winding (e.g. C309/C310) to "pad" it down to 125 kHz.Β  This forms a fairly wide (8-10 kHz) filter that rejects signals outside the immediate vicinity of its 125 kHz frequency.Β  Because this filtering is at a fixed frequency, it does not vary with input tuning which means that its bandwidth is constant over frequency.

Of all of the components in this device, this transformer is unique:Β  It was originally a 262.5 kHz IF transformer from a 1970s/1980s Philco (Ford) AM-only car radio.Β  While I could have certainly used the original 262.5 kHz frequency - or even 250 kHz, when I built this I decided to pad it down to 125 kHz using C309/C310Β  - a frequency that is conveniently 1/4th of the 500 kHz resonator.

It's been so long since I built this, I don't recall why I didn't simply divide the 500 kHz by two and readjust that transformer to 250 kHz.Β  Practically speaking, I could have also up-converted to 455 kHz and used either transformers or ceramic filters from a modern AM radio as 455 kHz ceramic resonators were certainly available at the time - but I didn't do that.

Each half of T301 has a center tap and to this, a bias voltage is applied via R315 to assure that the voltage on these switches was in the middle of the supply range, away from the protection diodes on the 4066's I/O pins, which could cause clipping/distortion should they be allowed to conduct if the signal voltage got too near the ground or supply rails.Β  To prevent coupling between the two halves of the transformer via the center tap, R314/C311 was added, the resistor adding isolation with the capacitor bypassing the remainder of the signal.Β  Practically speaking, being able to adjust the bias voltage was unnecessary as a simple resistive voltage divider to set the bias at 2.5 volts (1/2 the supply voltage) would have been just fine.

On the "other" side of the transformer is the other half of U6 (e.g. U6B/U6C) - this time, clocked from the fixed 125 kHz oscillator.Β  From this, the signal - previously converted up to 125 kHz is now converted back down to audio.

Post-mixer amp/LPF:

The output of the down-converting mixer is applied to U7B via R316, a 1k resistor and a 0.001uF capacitor, both of which form a simple R/C low-pass filter to attenuate any high-frequency leakage signals from the mixer.Β  Because the mixing process itself is a bit lossy (about 25% efficient) as is transformer/filter T301, U7B boosts the signal by a factor of 10 (20dB) and then applies it to U7A, which is configured as a variable gain amplifier section.Β  The output of this is then boosted again by U8, an LM386 which is capable of driving headphones or even a small speaker.

A few comments about the design:

Originally, the circuit lacked U7 at all, but it was added when the gain of U8 (the audio amplifier), by itself, was found to be inadequate.Β  Since U7 was "patched" into place, this explains the odd gain distribution:Β  If I were rebuilding this from scratch, I'd certainly not need two post-mixer amplifier sections and I could have likely eliminated one full dual op-amp package.Β  As it is, I may add a "high/low" gain switch somewhere around U5 to allow reduction of the gain somewhat when in the presence of possibly-high ultrasonic signal levels to prevent clipping prior to the band-pass filter which would surely degrade overall performance.

If I were to build this again I would likely use a 455 kHz IF, instead.Β  While not as plentiful, 455 kHz ceramic resonators are available to use for the BFO as are either transformer or ceramic-based band-pass filters.Β  I would also likely reconfigure U4B or U5 to perform the high-pass filter function rather than using harder-to-find inductors.

Again, I built this unit in the mid 1990s and have since lost my original notes, but I do recall that I modified it a few times since, simply tacking changes onto the old circuit rather than completely revising it.

Use as a longwave receiver:

While primarily intended to "hear" ultrasonic sounds such as those produced by bats, insects, leaking pipes, arcing power lines, etc., it is just a longwave radio receiver connected to a microphone:Β  If one connects a few 10s of feet/meters of wire to to J1 - and provides an Earth/ground reference to its shield connection - one can easily tune in the high-power transmitters used for submarine communications (around 20-30 kHz) plus the WWVB time signal at 60 kHz.Β  This must, of course, be done away from man-made noise sources such as power lines.

Alternatively, I have used a loop of about 1 foot (25cm) diameter of a dozen or so turns of wire along with a 10uF capacitor in series (to optionally block DC from R301) and been able to hear such signals - even in suburbia - but with this arrangement you'll also likely hear plenty of similar signals from the myriad switching supplies that likely inhabit your house as well!

Final comments:

The reader should be under no illusion that this is an optimized circuit or that I would do it this way again:Β  It was assembled fairly quickly to suit a need and to test a few random ideas, just to see if they would work.Β  Will I rebuild it at some point?Β  I don't know - it works as it should, so I don't plan to re-make something that is currently fit for purpose.

While I've heard very few bats with this - probably due to the deficiencies of the electret microphone at ultrasonic frequencies (which explains the future switch to MEMS-type microphones) - I've used it to find powerline noise (arcs are noisy at ultrasonic) and to test longwave receive antennas.

This page stolen from ka7oei.blogspot.com

[End]


LM2731 boost converter in Altium Designer – From schematic to PCB

18 September 2022 at 16:14

In this quick article, I show step by step process of drawing a boost converter schematic and finally ending up with a PCB layout. All of it done on Altium designer using Altium’s own...

The post LM2731 boost converter in Altium Designer – From schematic to PCB appeared first on Nuclearrambo.

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